Hi All
New day, new problem:
We have been on the road for 6 months now. Many places don't let you run a generator so it has been since September since I exercised ours.
I had a chance to run it here where we are. As usual, it took a few tries to get it to run but it started to run normally. I had two electric heaters set up so the genset had a load on it. It ran for about 3 minutes and I came in the coach and both heaters were running. The fridge had kicked over to AC so I know it was generating. Three minutes in it stopped. I had turned on one A/C unit at the time. Don't know if that was coincidence. Now it will kick over but will not run. There is plenty of oil in the pan so that is ruled out.
As a side, in September we were at a small RV park in California and their power went out on a day with temps in the low 100's. Their meter socket burned up. We are traveling with two cats so I started the genset to get the bus cooled down. It was surging badly from normal RPM's down to almost a stall. I ended up sticking an awl in the carb linkage to get it to run at a normal speed. Don't know if the two incidents are related.
New day, new problem:
We have been on the road for 6 months now. Many places don't let you run a generator so it has been since September since I exercised ours.
I had a chance to run it here where we are. As usual, it took a few tries to get it to run but it started to run normally. I had two electric heaters set up so the genset had a load on it. It ran for about 3 minutes and I came in the coach and both heaters were running. The fridge had kicked over to AC so I know it was generating. Three minutes in it stopped. I had turned on one A/C unit at the time. Don't know if that was coincidence. Now it will kick over but will not run. There is plenty of oil in the pan so that is ruled out.
As a side, in September we were at a small RV park in California and their power went out on a day with temps in the low 100's. Their meter socket burned up. We are traveling with two cats so I started the genset to get the bus cooled down. It was surging badly from normal RPM's down to almost a stall. I ended up sticking an awl in the carb linkage to get it to run at a normal speed. Don't know if the two incidents are related.